Thank you so much to all for your kindly comments.
Col, on the subject of Norfolk accents; these signs from around the Weybourne and Holt area made me roar when they were first installed:
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What a wonderfully inspired bit of humour to convey an otherwise serious message?
Apparently, such notices may have been of of little concern to me however, as a friend once pointed out: "You'll never get a speeding ticket the way you drive mate, but more likely fines for
long distance parking!"
Anyway, back to the project:
Everything seemed to be going swimmingly well, all things considered that is...?
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Uh, oh! An unforced error!
Having correctly located, drilled and tapped a hole in the boiler backhead for the lower gauge glass fittings, I had failed to note that the whole point of the firebox design is that it has to be removable for access to all the internal electric gubbins! Once the brassware was screwed firmly home, the top right lug would not draw out over the stud without contacting the back of the water cock!
Nuts! (pun intended)
The prospect of having to completely dismantle the entire gauge assembly for each occasion, with all the fine angle readjustments required in particular, was utterly unacceptable. A subtle solution was called for:
Fortunately, on the prototype, the clearance between the boiler plates and the firebox flange is so damn tight that the "dry" firehole casting has a near half circular cut out, just below that right upper lug, to accommodate the fitting. I reasoned that installing a flushed in and carefully shaped plate to the rear of the flange would allow the unit to be firmly attached and permanently aligned thus:
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At a first glance from the front, the bracket appears to be little more than a washer or shim beneath the nut when everything is bolted in place.
I was worried that the relatively thin plate might be rather vulnerable to accidental bending, so instead of my first consideration of using an M5 countersunk machine screw driven into the stem, I shaped down and threaded one end of a short length of 6mm rod to form a smooth stud. After opening out the hole in the backhead to a sliding fit there is hopefully more additional and adequate rigidity now?
Removal should be a reasonably simple process of undoing a cap nut on the steam cock and drawing out the "glass", plus a bit of jiggling with whatever protector type I finally choose to fit at a later date of course?!
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I had only taken a tiny nibble out of the precious 6mm rod, for the aforementioned stud, and remaining very keen to keep up the momentum, made a start on the three distinctive cock handles.
Nice, slender, tapered and curved rod affairs, scaled down and starting at 6mm diameter, reducing to 4mm with a fairly gentle 90 degree turn and back to 6mm for the spindle.
Quite a bit more filing and spinning to do... but I'm on a roll...!
Shaped up the first one, (took a while, as usual) grabbed the gas gun and applied lots of heat.
Started gently bending and...
BANG!
Started all over again.
New handle...
This time, keeping the flame on the bend...
BANG!
Lots of smoke after setting fire to the workshop floor where the broken handle section landed!
One more try?
Lightly peening it over with a small hammer...?
BANG!
"This ain't happened to me before?" (unusually polite version!)
Now there is not enough rod left in one piece for any more meaningful tries either, as sufficient extra material is required for gripping and leverage.
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It is not as if I had got much in the way of a turn before it failed either?
Incidentally, all three broke at precisely the same shallow angle of bend, hot and cold, rough and smooth...!!
Apparently, this stuff is a hard CZ121 brass, which it seems that all round, square and hex rod available is made out of anyway, so I have absolutely no idea what to do about this?!
From slightly stupefied in Suffolk?
Pete.